Jump to content

High End DIY Peristaltic - Masterflex Alternative?


TheClark

Recommended Posts

8 hours ago, albertareef said:

Congrats!  By comparison, 20 mls min was way higher than our standard lab applications. 

I have a punch list of things to fix, but there is promise here.

There is resonance in the case, it should be dead silent.  

The tubing moves.  Their design pins the tubing down with screws, but I think we can do better than that.  Seems like it would tear up the tubing over time.

 

cEj1hUt.png

 

The pump back siphons when not running.  I believe that increasing circumference of the pump head top portion will allow two rollers to be under more pressure and prevent that.

I put in an order for some geared stepper motors, my 100 dollar pump is getting spendy lol...

Hopefully when it is done, it will help others...

 

 

Link to comment
Share on other sites

On 11/16/2018 at 6:10 PM, albertareef said:

BTW - the tubing we used to get often had “stops” welded into it to prevent the creep across the heads - definitely a specialized part. 

Ok, more good info, wish I lived close it would be fun to pick your brain (ha, that is kind of a pun).

Many of my consumer grade pumps use fittings on the ends of the tygon, then these fittings snap into the pump.  Might be a bit cheaper than that option, but still intriguing!

 

  • Like 1
Link to comment
Share on other sites

3 hours ago, pdxmonkeyboy said:

if you made a wheel with 3 or 4 rollers wouldnt that stop the back siphoning? and increase flow?



Sent from my SM-G930V using Tapatalk
 

Ya, for sure!  It turns out, there are three rollers / bearings now.  The circle on the pump head that the rollers turn against is less than 50% of a circle if that makes sense?  I want it to be more like 75% based on my cheaper peristaltics lying around.  That ought to do the job.

Family visiting from out of town though, so this weekend is shot!

 

 

  • Like 1
Link to comment
Share on other sites

Ok, back at it tonight for a bit.  First off, here is the standard and the geared stepper.

 

4CC5E8C7-063D-4D3A-A834-156D32BBFA0E.jpeg

 

The geared stepper is powerful, a 5:1 reduction.  Even with efficiency loss it should be 4:1 effective worst case.

The gain in torque is excellent, but there were many changes such as the shaft size, connection points, dimensions.

This drove a need to redesign the pump head and attachment to the case.

So I modeled this up tonight.  

 

CadAnimation.gif

It is redrawn from scratch in fusion (working with STLs is a pita)...

The major changes are:

- New mounting points for the gear box

- New 8mm D shaft

- Increased diameter of rotation that rollers are engaged with the tubing (help with back siphon)

 

I hope to also add 

- keeper nuts for the pump top to hold it tighter and prevent threads from stripping out.

- keeper for the tubing better than a screw into the tubing (not a fan of that...)

- keeper on the shaft, just gotta find a place to fit it in...

 

Will print tonight and start iterating over the next few days until this thing pumps like a boss.

 

 

 

  • Like 2
Link to comment
Share on other sites

3 hours ago, SuncrestReef said:

Just curious...What's your background?  Are you a mechanical engineer by profession, or is this just a side hobby in addition to reefing?

Looks very cool!

Thanks!

Total side hobby like reefing. Like my signature Reef hacker at heart

Day job is software engineer. 

3d printing is amazing and I have learned so much including many hours of CAD via Fusion 360.  Highly recommend it to those who want to have even less of life :)

All the mechanical engineers like @Blue Z Reef and I think @Bicyclebill are probably biting their tongues looking at my amateur design.  However, this is a high leverage model from the original design, which sure helps.

  • Like 3
Link to comment
Share on other sites

So it looks like it's using 6 pressure wheels?  Should be able to get some reasonably smooth flow I would think.  Other tweaks to consider based on my memory of commercial units is having a groove in that top pressure cap to providing seating for the tubing.  You could even have alternate caps for different gauge tubbing to accommodate different flow ranges.  These are typically around half the depth of the tubing as I recall - which allows for 100 compression but helps support the tubbing more fully.  At least that is my recollection... granted it's been a while.  If I can find time at some point, I could try and dig some out of the basement at work and get some shots.

  • Like 1
Link to comment
Share on other sites

20 minutes ago, albertareef said:

So it looks like it's using 6 pressure wheels?  Should be able to get some reasonably smooth flow I would think.  Other tweaks to consider based on my memory of commercial units is having a groove in that top pressure cap to providing seating for the tubing.  You could even have alternate caps for different gauge tubbing to accommodate different flow ranges.  These are typically around half the depth of the tubing as I recall - which allows for 100 compression but helps support the tubbing more fully.  At least that is my recollection... granted it's been a while.  If I can find time at some point, I could try and dig some out of the basement at work and get some shots.

Dig some out and PM me for my address!  project cancelled!  Lol...

Yes, they allow for six bearings/rollers, but the as-built only shows 3.  I only have 3 bearings right now, they are spendy little suckers so I wanted to be sure.

Those are good ideas.  Most of the ones I have lying around here have a tubing channel, just not this design.

  • Haha 1
Link to comment
Share on other sites

Progress tonight!

The new pump assembly and motor works!  

 

5830F781-685C-4E0A-91A2-9A7E301F209A.jpeg

Items fixed:

- Plenty of torque

- Back siphoning fixed

- Motor runs cooler

- Motor runs quieter

It is so crazy accurate, impressive.

I was able to drive it up to 32 mls / minute.  My goal is about 150-200 as I run 128 mls/min right now.

It is going to require a new pump head and the larger tygon tubing I have on hand.  So back to CAD and back to ebay/ali/amazon for bigger bearings.

 

 

  • Like 1
Link to comment
Share on other sites

Keep up the good work! Would love to do one when you get the bugs figured out HaHa! I’d definitely need your help with the wiring/programming end of things...circuits was never my forte (hence why I’m not an EE/SE lol).

 

Honestly at 32 ml/min (roughly 12 plus gallons per day) would be great for a dual head auto water changer pump! 

 

If you need some acrylic cut out to fancy the final rig up (side covers or something), let me know, just need a 2D cad file and we’re good to go!

  • Like 1
Link to comment
Share on other sites

9 hours ago, Blue Z Reef said:

Keep up the good work! Would love to do one when you get the bugs figured out HaHa! I’d definitely need your help with the wiring/programming end of things...circuits was never my forte (hence why I’m not an EE/SE lol).

 

Honestly at 32 ml/min (roughly 12 plus gallons per day) would be great for a dual head auto water changer pump! 

 

If you need some acrylic cut out to fancy the final rig up (side covers or something), let me know, just need a 2D cad file and we’re good to go!

Thanks Jeff, will be glad to help.  I am hoping to do a custom PCB order to really simplify the wiring if enough people are interested. 

You have acrylic cutting connections too!  Nice :)

 

  • Like 1
Link to comment
Share on other sites

The not so glamorous side of 3d printing.  This was because my 'infill speed' was too high for the nozzle size in use.  It couldn't melt plastic fast enough.

FF1BE7DE-7485-4948-BD6D-D954B0803294.jpeg

 

 

Fast forward to a good looking, working version (on right)

676DBB6E-6C3A-43A1-8E34-048ECA7B1B78.jpeg

 

Now I gotta say, these version is HUGE!.  Seems like I am going to lose 50% of the gearing advantage by going this big (2x diameter of original).  Mechanical engineers please confirm :)

These 608 bearings are just too huge...

Ah well, might as well finish it off and see...

 

  • Like 1
Link to comment
Share on other sites

  • 3 weeks later...

Been working in the evenings on a completely new set of pump hardware.  This is brand new from scratch, nothing to do with the original pump hardware.

Still a work in progress, but here is a render:

- Smaller, better gearing ratio.

- Rotors lock together like a puzzle, reinforced with screws through middle of shaft

- Able to run the 10mm tubing

- Bolts directly onto the motor, the motor shaft gives the whole pump rotor strength

- Designed to be bolted onto a geared stepper motor, for plenty of power

- Tubing locks into place in housing, tubing will not drift while pumping

PeristalticRemovableHead v15.png

  • Like 3
Link to comment
Share on other sites

7 hours ago, TheClark said:

Been working in the evenings on a completely new set of pump hardware.  This is brand new from scratch, nothing to do with the original pump hardware.

Still a work in progress, but here is a render:

- Smaller, better gearing ratio.

- Rotors lock together like a puzzle, reinforced with screws through middle of shaft

- Able to run the 10mm tubing

- Bolts directly onto the motor, the motor shaft gives the whole pump rotor strength

- Designed to be bolted onto a geared stepper motor, for plenty of power

- Tubing locks into place in housing, tubing will not drift while pumping

PeristalticRemovableHead v15.png

Cool!  I want to see this bad boy up and running.  Curious to see what kind of flow rate range you achieve with your motor choice.

Link to comment
Share on other sites

1 hour ago, albertareef said:

Cool!  I want to see this bad boy up and running.  Curious to see what kind of flow rate range you achieve with your motor choice.

Thanks!  It's working!  Going to make one change to the housing to keep the rollers engaged a few more degrees in the rotation.

My goal is around 100 mls/min, but with the pump turning slow.  Idea is, that the tubing should last longer for the same amount of mls pumped.  Theory is moving slow is less wear on the tubing.  It is looking very good!

Still gotta design a new case for the electronics, but this is a huge step forward.

Link to comment
Share on other sites

Join the conversation

You can post now and register later. If you have an account, sign in now to post with your account.
Note: Your post will require moderator approval before it will be visible.

Guest
Reply to this topic...

×   Pasted as rich text.   Paste as plain text instead

  Only 75 emoji are allowed.

×   Your link has been automatically embedded.   Display as a link instead

×   Your previous content has been restored.   Clear editor

×   You cannot paste images directly. Upload or insert images from URL.

Loading...
×
×
  • Create New...